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Plane crashes into Snake River near Porterville Bridge in Bingham County
Nate Sunderland, EastIdahoNews.com
BLACKFOOT — Bingham County Sheriff deputies
responded to a plane crash in the Snake River Sunday evening near the area of the Porterville Bridge.
Initial information received indicated the pilot, and sole occupant of the aircraft, had made contact at a nearby residence at about 6 p.m. to ask for help. He had suffered non life-threatening injuries, according to a Bingham County news release.
The pilot, whose name has not been released, was treated at Eastern Idaho Regional Medical Center in Idaho Falls, according to Bingham County Sheriff Chief Deputy Jordyn Nebeker.
Emergency responders arrived at the scene to address the logistics of retrieving the aircraft. For safety reasons, the plane will remain at the scene until Monday morning. The aircraft is secure in the water, and clearly visible, Nebeker said.
The Porterville Bridge was closed for approximately 45 minutes to safely gain access to survey the scene. There is no reported damage to the bridge itself.
Nebeker was unaware of the exact type of aircraft involved in the crash, but that information is expected to be released after an investigation by the Federal Aviation Administration.
The plane will be removed Monday morning, Nebeker said.
Bingham County is asking residents not to call dispatch to the report the plane on Monday, as they are well aware of its location.
EastIdahoNews.com will update this story as more details on the crash are reported.
Plane crashes into Snake River near Porterville Bridge in Bingham County
One dead, two critically injured after LifeFlight helicopter crash in Wilson County
By: Holly Lehren
WILSON COUNTY, Tenn. (WTVF) — Vanderbilt
University Medical Center has confirmed that one crew member was killed and two others were seriously injured after a LifeFlight helicopter crashed Saturday afternoon in Wilson County.
The helicopter, LifeFlight 1, went down in an unpopulated area near the 7100 block of Cairo Bend Road around 2 p.m. Officials said the aircraft had taken off from the Wilson County Emergency Operations Center at 1:33 p.m. and was not carrying a patient at the time.
In a statement, Vanderbilt Deputy Chief Executive Officer and Chief Health System Officer Dr. Jane Freedman said Flight Nurse/Paramedic Allan Williams did not survive. Critical Care Flight Paramedic Andrew “Andy” Sikes and the pilot, whose family requested privacy, were seriously injured and remain hospitalized.
“For 41 years, through more than 80,000 flights and 40,000 ground transports, the remarkable members of the Vanderbilt LifeFlight team have saved countless lives,” Dr. Freedman said. “Despite the inherent risk of this work, these dedicated individuals feel called to serve patients in their most vulnerable moments.”
Dr. Freedman asked the community to “join me in support of [Allan’s] family, as well as Andy, the pilot, and their families” as the organization grieves this loss.
The FAA and NTSB are investigating the crash.
https://www.newschannel5.com/news/medical-helicopter-crashes-in-wilson-county-crews-responding
Small plane crashes in field near Pacific school
by KOMO News Staff
PACIFIC, Wash. — A small plane that took off from
Shady Acres Airport in Pierce County was destined for Auburn Airport and made an unexpected landing in an empty field near a school in Pacific, Friday afternoon, after it lost power, police said.
The plane with a 43-year-old pilot and a 74-year-old passenger crashed and landed near Alpac Elementary in the 3100 block of Milwaukee Blvd N, according to officials.
Pacific police and Valley Regional Fire confirmed that the two people inside the plane emerged unscathed.
The plane ended up upside down, and the FAA and NTSB will handle the investigation, according to the Pacific police.
Small aircraft makes emergency landing on I-15 outside of Jean, no injuries reported
by News 3 Staff
A four-seater single-engine aircraft with two
occupants made an emergency landing on the northbound lanes of Interstate 15, 14 miles north of the Nevada/California state line, after experiencing engine failure.
Fortunately, neither the occupants nor anyone on the ground sustained injuries.
As a result of the incident, all northbound traffic is being diverted off the Interstate at the Jean, Nev., exit to State Route 604.
The Federal Aviation Administration has been notified of the situation.
All In Aviation, whose flight was involved in the emergency landing, sent in this statement to News 3,
Small plane crash in Boise leaves no serious injuries; drivers urged to avoid area
by CBS2 News Staff
BOISE, Idaho (CBS2) — Boise Police and Fire are
responding to a small plane crash near Orchard, Victory, and W. Wright Street.
The crash involved two passengers. Police say there are no life-threatening injuries reported.
Authorities are advising drivers to steer clear of the area.
The incident has not affected airport operations.
Small plane crash-lands at Ludington Pump Storage reservoir
By Michelle Fedder, Editor
MASON COUNTY — An investigation is underway
after a small airplane crashed near the Ludington Pump Storage Plant this weekend.
Emergency crews were dispatched at about 2:13 p.m. on Saturday to the 3500 block of South Lakeshore Drive after an “iPhone crash detection” alert, according to a Sunday news release from the Mason County Sheriff’s Office.
“While responding to the call, the Mason/Oceana County 911 Center received a call from the pilot reporting the crash and that there were no injuries” to himself or his 83-year-old passenger from Muskegon, reads the news release.
The pilot, a 61-year-old man from Issaquah, Washington, told law enforcement that he was flying to Ludington from Fremont. The pilot said that “between 2,700 feet and 3,500 feet the plane’s engine seized. The pilot reported turning the aircraft into the wind and started to descend.”
The pilot reportedly made a controlled landing on top of the Ludington Pump Storage reservoir. After landing, the aircraft slid down the embankment, coming to rest at the bottom of the hill on the west side of the reservoir, according to police.
No fuel leaks were reported or observed, and the National Transportation Safety Board was notified, according to the release.
The NTSB is an independent federal agency that investigates and determines the probable causes of “every civil aviation accident in the United States and significant events in the other modes of transportation — railroad, transit, highway, marine, pipeline and commercial space.”
Troopers from the Michigan State Police Hart Post and Michigan Department of Natural Resources law enforcement assisted the sheriff’s office at the scene.
https://www.ourmidland.com/news/article/ludington-plane-crash-21150054.php
NTSB Final Report: Arlie L Raber III Challenger 1
Pilot Was Having Difficulty Controlling The Airplane’S Rudder Pedals Due To His Physical Stature
Aviation Investigation Final Report
Location: Crestview, Florida Accident Number: ERA25LA197
Date & Time: May 4, 2025, 14:20 Local Registration: N59BR
Aircraft: Arlie L Raber III Challenger 1 Aircraft Damage: Substantial
Defining Event: Loss of control in flight Injuries: 1 None
Flight Conducted Under: Part 91: General aviation - Personal
Analysis: The pilot was having difficulty controlling the airplane’s rudder pedals due to his physical stature. After several taxi attempts up and down the runway, he elected to take off for a short flight. After becoming airborne, the pilot began to have yaw controllability problems. He attempted to land, but was unable to control the airplane’s movements effectively, as his knees were contacting the instrument panel, and his feet were wedged behind the rudder pedals. The airplane continued to fly over terrain about 6 feet above ground level. With trees approaching, the pilot pushed the nose of the airplane down resulting in a hard landing. The airplane sustained substantial damage to the forward portion of the fuselage and the left wing.
The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s decision to take off despite having problems controlling the airplane due to his physical stature.
FMI: www.ntsb.gov
NTSB Final Report: Piper PA-44-180
While On The Base Leg Of The Airport Traffic Pattern The Right Main Landing Gear Did Not Fully Extend
Location: Pompano Beach, Florida Accident Number: ERA25LA096
Date & Time: January 10, 2025, 11:15 Local Registration: N555HF
Aircraft: Piper PA-44-180 Aircraft Damage: Substantial
Defining Event: Sys/Comp malf/fail (non-power) Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Flight test
Analysis: Both pilots reported that after performing airwork they returned to the departure airport where multiple uneventful full stop landings were performed. They then departed and while on the base leg of the airport traffic pattern the right main landing gear did not fully extend. At that point the designated pilot examiner (DPE) took the controls from the pilot applicant, and during the course of 90 minutes, made multiple attempts to fully lower the right main landing gear that were ultimately unsuccessful. The DPE then elected to land with the landing gear retracted rather than with two landing gear down and one retracted. After touchdown the airplane came to rest near the runway centerline. The underside of the fuselage was substantially damaged during the landing.
After raising the airplane from the runway, the right main landing gear was manually pulled out of the wheel well and during that process it was discovered that the hardware that secured the upper and lower torque links were not in position and could not be located. Since the hardware could not be found, no determination could be made as to the reason for the separation of the hardware. A review of the airplane’s maintenance records revealed that the hardware securing the right main landing gear torque links was replaced last on about 11 months before the accident. At the time of the accident, the airplane had accrued about 324 flight hours since the hardware replacement. The mechanic who performed the last 100-Hour inspection, about 6 months and 46 hours before the accident, reported that he did not notice any abnormality or defects with the torque link bolts at that time.
Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The separation of the securing hardware for the right main landing gear upper and lower torque links for undetermined reasons, which prevented extension of the right main landing gear.
FMI: www.ntsb.gov
NTSB Prelim: Siai-Marchetti SM 1019
As The Pilot Turned Onto Final For Runway 19, He Noticed That The Engine RPM Oscillations Became More Erratic
Location: Richland, WA Accident Number: WPR26LA006
Date & Time: October 2, 2025, 10:50 Local Registration: N3172U
Aircraft: Siai-Marchetti SM 1019 Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Personal
On October 2, 2025, about 1050 Pacific daylight time, a Siai-Marchetti SM 1019, N3172U, sustained substantial damage when it was involved in an accident near Richland, Washington.
The pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot reported that he departed Tri-Cities Airport (PSC), Pasco, Washington, on a local flight. About 45 minutes into the flight, he observed uncommanded engine rpm oscillations and decided to make a precautionary landing at Richland Airport (RLD), Richland, Washington.
While on the downwind leg for runway 19, as the pilot moved the condition lever forward, it felt like the propeller was moving unsolicited, from beta to flight idle. He recalled that when he tried to return the propeller from beta, to flight idle, the engine rpm oscillations increased significantly.
As the pilot turned onto final for runway 19, he noticed that the engine rpm oscillations became more erratic. The pilot stated that when the propeller felt like it had entered beta, the airspeed decreased below the airplane’s stall speed and thrusted the occupants forward in their seats. Subsequently, the pilot lowered the nose added power and noted that the slightest increase of the power control lever resulted in an extreme engine rpm increase followed by the nose of the airplane pitching upward. He applied 15° flaps and slowed the airplane to about 50 knots.
The pilot stated that after touchdown, the landing roll was normal for about 50 ft. As he applied brakes, the engine rpm increased and the airplane became airborne. Subsequently, the airplane turned left, touched down hard on the runway, and the right main landing gear collapsed. Subsequently, the airplane exited the left side of the runway and came to rest upright. Postaccident examination of the airplane revealed that the right wing was substantially damaged. The airplane was recovered to a secure location for further examination.
FMI: www.ntsb.gov

Today in History
63 Years ago today: On 10 November 1962 An Air Vietnam Douglas DC-3 impacted a mountain while on approach to Da Nang Airport, Vietnam , killing all 27 occupants.
| Date: | Saturday 10 November 1962 |
| Time: | 14:37 |
| Type: | Douglas C-47B-25-DK (DC-3) |
| Owner/operator: | Air Vietnam |
| Registration: | XV-NID |
| MSN: | 32822/16074 |
| Year of manufacture: | 1945 |
| Engine model: | P&W R-1830-90C |
| Fatalities: | Fatalities: 27 / Occupants: 27 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed, written off |
| Category: | Accident |
| Location: | 20 km NNW of Da Nang Airport (DAD) - Vietnam |
| Phase: | Approach |
| Nature: | Passenger - Scheduled |
| Departure airport: | Hue-Phu Bai Airport (HUI/VVPB) |
| Destination airport: | Da Nang Airport (DAD/VVDN) |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:
An Air Vietnam Douglas DC-3 impacted a mountain while on approach to Da Nang Airport, Vietnam , killing all 27 occupants.
The Air Vietnam DC-3 took off from Hue at 0620 GMT for a flight to Da Nang. After some difficulties in establishing radio communications with Da Nang, the flight obtained weather conditions and runway in use at Da Nang. The DC-3 crew replied that they would report on the downwind leg of runway 35. Da Nang requested the plane's position and ETA, but received no reply. The wreckage was later found on a mountain at an elevation of 550 m, 19,6 km NW of Da Nang Airport.
PROBABLE CAUSE: "The accident probably resulted from a navigational error in adverse meteorological conditions."
