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Today is Tuesday the 10th of March, 2026

From day one of the 2026 ARFF Leadership Symposium in Addison, Texas, here are your stories for today...

Be safe out there!

Tom

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One Person Killed in Helicopter Crash outside Mojave

Patti Orr

MOJAVE – One person was killed when a helicopter crashed just outside of Mojave, the incident occurred on the afternoon of March 9th near Oak Creek Road and 90th Street West.

According to the CHP traffic information page, a call came into the Bishop Dispatch Center at approximately 3:21pm for a helicopter down and on fire. When the Kern County Fire Department out of Tehachapi and Mojave arrived, they located the downed aircraft and quickly extinguished the blaze which also caused a small brush fire in the adjacent area; fire officials confirmed one person on board was killed in the crash.

The Mojave area CHP contacted the FAA (Federal Aviation Administration) and were already in contact with the Kern County Sheriff’s Department, both agencies immediately contacted the NTSB (National Transportation Safety Board).

NTSB investigators are headed to the crash site to investigate the cause of the crash and in a quick statement, the NTSB did say that “The helicopter which is a MD Helicopter 369FF rapidly descended into terrain while laying powerlines,”

At this time, it’s unclear how many were on board the aircraft; this is a developing story, and we’ll have more information as it develops so, stay tuned.

https://www.desertnews.com/news/article_8c807219-05e7-4531-9028-ae357af5a0bd.html

Two transported to hospital after small plane crash in Arizona

by: Amelia Hobson

MOHAVE COUNTY, Ariz. (ABC4) — Two people were injured after a small plane crash near the Utah border earlier Monday.

According to the Mohave County Sheriff’s Office (MCSO), they responded to the area of Arizona Strip Road, approximately 15 miles across the Utah-Arizona border after reports of a plane crash.

The aircraft was a small personal plane with two occupants. The two occupants reportedly experienced minor injuries and were transported to the hospital in stable condition. At this time, officials have not identified them.

At this time, it has not been determined what happened leading up to the incident, and Anita Mortensen with MCSO said the investigation is being transferred to the Federal Aviation Administration and the National Transportation Safety Board for investigation.

Officials have also not disclosed if the plane was damaged in the incident or the extent of any damage.

https://www.abc4.com/arizona/two-transported-hospital-plane-crash-arizona/

NTSB Prelim: Cessna 177

The Airplane Had Been Undergoing Maintenance For The Past 11 Months Following A Propeller Strike

Location: Ocoee, TN Accident Number: ERA26LA093
Date & Time: January 13, 2026, 15:30 Local Registration: N34959
Aircraft: Cessna 177 Injuries: 1 Minor
Flight Conducted Under: Part 91: General aviation - Personal

On January 13, 2026, about 1530 eastern standard time, a Cessna 177B, N34959, was substantially damaged when it was involved in an accident near Ocoee, Tennessee. The pilot received minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to the pilot, the airplane had been undergoing maintenance for the past 11 months following a propeller strike. The repairs and the annual inspection were completed the day before the accident flight. After refueling the fuel tanks and performing a preflight inspection,
with no anomalies observed, he departed from Lovell Field Airport (CHA), Chattanooga, Tennessee, and proceeded east. About 20 minutes after departure, and at an altitude of 4,500 ft mean sea level (msl), the engine rpm increased to 3,000 rpm, which is 300 rpm above the engine’s maximum operating rpm, followed by an engine vibration. The pilot declared an emergency to air traffic control but determined he would be unable to reach the nearest airport and initiated a forced landing in a field. During the landing rollout, the airplane continued into a wooded area and impacted trees.

Postaccident examination of the airplane revealed it had sustained substantial damage to the wings, the fuselage, and the horizontal stabilator. A coating consistent with engine oil was observed on the left side of the engine and fuselage.

The wreckage was retained for further examination.

FMI: www.ntsb.gov

Today in History

7 Years ago today: On 10 March 2019 Ethiopian Airlines flight ET302, a Boeing 737 MAX 8, crashed shortly after takeoff from Addis Ababa-Bole Airport, Ethiopia. There were no survivors among the 157 occupants.

Date: Sunday 10 March 2019
Time: 08:44
Type: Boeing 737 MAX 8
Owner/operator: Ethiopian Airlines
Registration: ET-AVJ
MSN: 62450/7243
Year of manufacture: 2018
Total airframe hrs: 1330 hours
Cycles: 382 flights
Engine model: CFMI LEAP-1B
Fatalities: Fatalities: 157 / Occupants: 157
Other fatalities: 0
Aircraft damage: Destroyed, written off
Category: Accident
Location: 50 km ESE of Addis Ababa-Bole Airport (ADD) -    Ethiopia
Phase: En route
Nature: Passenger - Scheduled
Departure airport: Addis Ababa-Bole Airport (ADD/HAAB)
Destination airport: Nairobi-Jomo Kenyatta International Airport (NBO/HKJK)
Investigating agency:  AAIB Ethiopia
Confidence Rating:  Accident investigation report completed and information captured

Narrative:
Ethiopian Airlines flight ET302, a Boeing 737 MAX 8, crashed shortly after takeoff from Addis Ababa-Bole Airport, Ethiopia. There were no survivors among the 157 occupants.

Takeoff roll began from runway 07R at 08:38 hours local time, with a flap setting of 5 degrees and a stabilizer setting of 5.6 units.
At 08:38:44, ten seconds after rotation, the left and right recorded Angle of Attack (AOA) values deviated. The left AOA decreased to 11.1° then increased to 35.7° while value of right AOA indicated 14.94°.
This resulted in the onset of the stick shaker followed by a master caution light. At the same time the captainÂ’s primary flight display (PFD) showed a drop in indicated airspeed (IAS) from 170Kt to 156Kt.
The captain initially responded by reducing the pitch as a reaction to the stick shaker. This did not stop the stick shaker and the captain to stopped applying further nose down column input at a pitch angle of 7-8° above horizon
Approaching 400 ft, the captain attempted to engage the autopilot (AP) but it was not successful. A second attempt failed as well. Passing 1000 ft radio altitude, at the third attempt, the autopilot was successfully engaged.
The captain asked the first officer to advise ATC of the inability to follow the planned departure due to a flight control problem and to request runway heading and climb 14,000ft.
The left stall management yaw damper computer which was affected by inputs from a failed left AOA sensor calculated the left hand minimum operational airspeed erroneously above 340kt (VMO). This resulted in an overspeed warning.
At the same time, the auto throttle operation was affected by the erroneous left AOA sensor value and remained in the Arm mode and failed to transition to N1 mode, which would have reduced the take-off thrust to climb thrust automatically.
The auto throttle did not give a warning or a failure flag for the flight crew when its operation was affected by the failed AOA sensor value.
The first activation of the Maneuvering Characteristics Augmentation System (MCAS) system occurred within a second where the auto throttle was supposed to reduce from take-off thrust to climb trust. And in less than another second the GPWS aural alert "DONÂ’T SINK" sounded twice.
The activation of MCAS followed by GPWS aural alert with already ongoing stick shaker coupled with no failure flag or warning from the auto throttle in an extremely high workload environment must have caused the auto throttle remaining in the ARM mode with take-off thrust set to remain unnoticed by the crew.
At 08:39:45, captain requested flaps up and the first officer moved the flap handle to position 0. The autopilot then disengaged and the flaps reached the up position.
At 08:40:00, because of the erroneous left AOA value, the MCAS activated the first automatic nose down trim for 9 seconds. At the end of the first MCAS activation the stabilizer position was 2.1 units with the captain pulling to pitch up the airplane, with a force of around 90 lbs (41 kg). At different times when the pilot applied electrical trim for short duration or longer duration the trim stopped at about 2.3 for unknown reasons.
At 08:40:20 the second MCAS activation, lasting 7 seconds, was interrupted by the captainÂ’s electric trim up inputs. The captain applied a nine second electric trim-up input which fully counteracted the second MCAS input and stopped the GPWS warning but it did not bring the aircraft to a neutral trim condition.
When MCAS activated for the third time an automatic nose-down trim was commanded there was no corresponding motion of the stabilizer, which is consistent with the stabilizer trim cutout switches being in the Â’cutoutÂ’ position.
The captain repeatedly requested the first officer to pull up with him on the control column with pitch values oscillating between 7° nose up and -2° nose down. Pitch increased when both pilots applied forces, pitch decreased when a single pilot applied force (force oscillated between 80
lbs and 110 lbs (36-50 kg)). The vertical speed variations followed the variations of the pitch angle, with vertical speed was oscillating between -2,500 ft/min and 4,400 ft/min.
The captain requested the first officer to try the manual trim wheel, and after seconds of intense efforts, the first officer told the captain that it was not working. This was due to the amount of force required to turn the trim wheel. At this moment the stabilizer trim was at 2.3 units with the IAS at 340 Kts.
At 08:42:10 the captain asked and the first-officer to request radar control a vector to return. ATC instructed ET302 to turn right heading 260 degrees. During the radio communications with the ATC, the first officerÂ’s action on the control column was released which increased forces on the captainÂ’s control column. The captain then requested the first officer to check the Master Caution. Then, they both announced "left alpha vane".
At this time the airplane was almost reaching the minimum safe altitude. After about 10 seconds the captain then told the first officer that they should pitch up together. The captain then told the first officer "pitch is not enough" and "put them up". A sound similar to stab trim cut-out switches being returned to normal was recorded on the CVR, thus the stab trim cut out switches were most likely turned back on at that moment.
After a failed attempt to trim using the manual trim wheel as per the runaway stabilizer non-normal checklist and significant and unbearable amount of force on the control column, the flight crew were trying to find other means to relieve the force. The airplane was at 13800 ft; IAS was 367kt, pitch just below 1°, stabilizer at 2.3 units of trim, bank angle 21° right.
The crew was busy pulling on the controls with high muscular force trying to maintain airplane flight path control and reach 14000 ft, a target on which they remained focused. Trying to maintain flight path control was a very demanding task and represented here a high workload, physically and mentally, to the detriment of every other task.
An overspeed warning added another disruption and disturbance on board. The cockpit noise environment was unsettling and further impacted the flight crewÂ’s concentration.
Immediately after the stab trim cut-out switches were put back in normal position, the crew attempted another unsuccessful autopilot engagement as the plane was approaching 14000 ft. At the same time, the captain applied two brief electric trim up inputs of 1 second each while pulling on the control with an average force of 100 Lbs (45 kg). The force on the controls remained between 75 and 100 Lbs.
At 08:43:20, five seconds after the trim-up inputs, the fourth MCAS triggered. The plane started to descend. During the 9-second MCAS activation, the stabilizer decreased from 2.3 units to 1 unit of trim. The captain repeatedly shouted to the first officer to pitch up. The forces were physically unmanageable by both flight crews. The aircraft began pitching nose down.
The airplane hit the ground eighteen seconds after the end of the 4th MCAS.

The investigation noted that intermittent flight control system abnormalities began well before the accident flight. Maintenance actions of relevance started occurring in December 2018 when the airplane was one month old and included several pilot write ups involving temporary fluctuations of vertical speed and altitude. There were also three reports of the airplane rolling during autopilot operation. Altitude and vertical speed indications on the PFD showed erratic and exaggerated indications.
From the maintenance log book report the airplane also suffered intermittent electrical/electronic anomalies in addition to the flight control system malfunctions. For example, three days before the crash the Auxiliary Power Unit (APU) Fault Light illuminated, and the APU had a protective shutdown. The onboard maintenance function computer message also indicated the Start Converter Unit (SCU) showed the APUÂ’s start system was inoperative. The SCU is located in the electrical and electronics (E/E) compartment. The captainÂ’s personal computer power outlet also had no power. The possibility of intermittent electrical/electronic system defects were an underlying issue.
The AOA sensor malfunction on the accident flight most likely occurred as the result of a power quality problem that resulted in the loss of power to the left AOA Sensor Heater. Evidence indicates the loss of power was likely due to a production related intermittent electrical/electronic failure involving the airplaneÂ’s Electrical Wiring Interconnection System (EWIS) and the AOA Sensor part.

Probable cause of the accident
Repetitive and uncommanded airplane-nose-down inputs from the MCAS due to erroneous AOA input, and its unrecoverable activation system which made the airplane dive with the rate of -33,000 ft/min close to the ground was the most probable cause of the accident.

Contributing Factors
1. The MCAS design relied on a single AOA sensor, making it vulnerable to erroneous input from the sensor;
2. During the design process, Boeing failed to consider the potential for uncommanded activation of MCAS, but assumed that pilots would recognize and address it through normal use of the control column, manual electric trim, and the existing Runaway Stabilizer NNC. The OMB and Emergency AD issued after the Lion Air accident included additional guidance but did not have the intended effect of preventing another MCAS-related accident;
3. While Boeing considered the possibility of uncommanded MCAS activation as part of its FHA, it did not evaluate all the potential alerts and indications that could accompany a failure leading to an uncommanded MCAS;
4. The MCAS contribution to cumulative AOA effects was not assessed;
5. The combined effect of alerts and indications that impacted pilotÂ’s recognition and procedure prioritization were not evaluated by the Manufacturer;
6. Absence of AOA DISAGREE warning flag on the flight display panels (PFD);
7. The B737 MAX Crew difference CBT training prepared by Boeing and delivered to Pilots did not cover the MCAS system;
8. Failure by the manufacturer to design simulator training for pilots with regards to safety critical systems like MCAS with catastrophic consquences during undesired activation.
9. The manufacturer failed to provide procedures regarding MCAS operation to the crew during training or in the FCOM;
10. Failure by the manufacturer to address the safety critical questions raised by the airline which would have cleared out crew confusion and task prioritization.

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