Hope everyone had a great 4th of July, no lost appendages and now with clear heads!
We start the new week with the following stories...
Of note, today is the 13 anniversary of Asiana Airlines flight 214 where a Boeing 777-200 was destroyed in a landing accident at San Francisco International Airport, California (SFO). There were 291 passengers and 16 crew members on board. Three passengers died and 48 were seriously injured.
Be safe out there!
Tom
--
Seaplane carrying 8 passengers crashes into NYC’s East River
By Steven Vago, Joe Marino, Zoe Hussain and Ronny Reyes
A seaplane carrying eight people crashed into New York City’s East River on Sunday, with emergency responders rushing to the scene, video shows. 
Footage of the river shows the plane bobbing in the water with one wing submerged as rescue crews work to get the passengers out.
The plane took a hard landing in the choppy waters and partially capsized at just after 12 p.m., officials told The Post.
Eight people were rescued from the plane by the FDNY. Two passengers with minor injuries were evaluated by emergency medical staff, officials said.
The crash unfolded near the Manhattan ferry and Skyport terminal along 23rd Street and FDR Drive.
After the passengers were removed from the plane, the ship was put upright on the water and towed back to the docks.
At least five ships were seen aiding in the response, with another seaplane spotted nearby. 
Recreational boater Dan Thys and his wife were on the closest ship to the downed plane — and were the first to respond.
The couple was cruising down the East River toward New York Harbor in their Eastbay 43 express cruiser to try to catch an armada of tall ships that set sail on Saturday for July 4th when the seaplane suddenly crashed — causing them to leap into action.
Thys, of Pelham, recalled noticing the plane abort a landing and attempt to take off again, then try to land in the opposite direction, before the harrowing accident unfolded.
“We were cruising; we were going down into the harbor. And since we were the closest vessel next to the plane, we went right over, and one of the pilots was standing … on one of the floats,” Thys told The Post.
The pilot accepted Thys’ offer for help, which included handing over life jackets, but an NYPD rescue boat quickly took over and the boater moved out of the way.
“He — I’m sure — was a little shaken,” Thys said of the pilot. “The first thing that rang through our mind is how can we help?” 
“And then very shortly thereafter the NYPD came up, and they told us they were taking over and so we backed off and let the NYPD take care of it,” he said.
Thys noted that the waters were “fairly rough” and that the journey into the harbor was a “very, very bouncy ride.”
Pictures taken by Thys captured the pilot crouching on a float beside the partially submerged seaplane as an NYPD boat approached the aircraft.
“It’s an unusual experience. I hope it won’t happen again. I read that there are two people who were injured. I don’t know what the injuries are, but I hope everybody’s OK.”
An investigation into the crash remains ongoing, police said.
The incident comes less than a month after another seaplane was rescued from the East River after it was struck by a wave during takeoff and left it struggling in the water near the Throgs Neck Bridge.
https://nypost.com/2026/07/05/us-news/seaplane-carrying-10-passengers-crashes-into-nycs-east-river/
Small plane has ‘hard landing’ on SR-60 after hitting powerlines: PCSO
By Lindsey Gimbert
The Brief
-
- The Polk County Sheriff's Office assisted in diverting traffic after a small plane crashed on State Road 60.
-
- According to PCSO, the ultralight plane experienced a ‘hard landing’ shortly after takeoff.
-
- The two occupants of the plane are expected to be okay.
MULBERRY, Fla. - The Polk County Sheriff’s Office said
deputies are redirecting traffic around an ultralight plane that crashed on State Road 60.
PCSO said around 11:30 a.m. the ultralight plane crashed shortly after takeoff when it hit several power lines. The pilot and the passenger, a father and son, were transported to the hospital and are expected to be okay.
Deputies say the eastbound lanes of 60 opened shortly after the crash as they directed westbound traffic via the eastbound lanes.
What we don't know:
It is unclear why the ultralight plane hit power lines after takeoff.
https://www.fox13news.com/news/small-plane-has-hard-landing-sr-60-after-hitting-powerlines-pcso
Small plane goes off runway at Kelowna Airport
YLW reopens after mishap
Madison Reeve
UPDATE: 12:15 p.m.
Kelowna International Airport is resuming regular operations after emergency crews removed a small plane that went off the runway. 
The airport was closed to all inbound and outbound flights for nearly an hour while crews dealt with the plane.
Some flights were rerouted while a few others returned to their city of origin.
Airport officials ask that you check with your airline before venturing to the airport to determine the status of your flight.
UPDATE: 11:55 a.m.
All air traffic in and out of Kelowna International Airport has been halted while emergency crews deal with a small plane that went off the runway.
All flights presently inbound from other cities have either returned to their city of origin, or have been diverted to other airports.
The Porter Airlines flight 321 from Toronto has landed in Vancouver after circling YLW for several minutes.
Airport officials tell Castanet News regular traffic will resume once the runway is clear.
As of 11:55 a.m. the aircraft had just been removed from the runway.
We will have more information concerning resumption of airport operations.
In the meantime, people are asked to check with their airline before heading to the airport.
ORIGINAL: 11:10 a.m.
A small plane experienced difficulty while landing at Kelowna International Airport on Friday morning.
A witness told Castanet the aircraft, believed to be carrying two people, went off the runway.
The Kelowna Fire Department responded to the scene.
The incident has caused delays for several arriving flights. Two flight out of Toronto and a flight from Calgary and one from Vancouver are circling the airport while awaiting clearance to land.
It is not yet known whether the runway or tarmac has been temporarily closed.
Castanet has reached out to Kelowna International Airport for more information and will update this story as details become available.
https://www.castanet.net/news/Kelowna/622984/Small-plane-goes-off-runway-at-Kelowna-Airport
Two Injured After Small Aircraft Crashes Near High River Regional Airport In Alberta
Aviation Today News Desk
Alberta, Canada: Two men were seriously injured after a small aircraft crashed in a field east of the High River Regional Airport in Alberta on Thursday afternoon, prompting a multi-agency emergency response and an investigation by Canadian aviation authorities. 
The crash was reported at approximately 3:45 p.m. local time in a grassy area east of the airport in Foothills County, near High River, according to emergency officials. RCMP, High River Fire Department personnel and Alberta Health Services crews responded to the scene shortly after receiving reports of a downed aircraft.
Emergency responders located the aircraft in a field between 554 Avenue and 594 Avenue, east of the airport. Both occupants identified only as two adult men were extricated from the wreckage and transported by ground ambulance to Foothills Medical Centre in Calgary with serious injuries. Authorities said the injuries were significant but not believed to be life-threatening, and both men were expected to survive.
Officials described the aircraft only as a single-engine, single-propeller airplane. As of the latest official updates, authorities have not released the aircraft’s make, model, registration, owner or operator, nor have they identified the two occupants or confirmed the purpose of the flight. No information has been released regarding the aircraft’s departure point or intended destination.
The circumstances leading to the crash remain under investigation. Officials have not indicated whether the aircraft experienced a mechanical problem, engine failure, weather-related issue, or pilot emergency before coming down. There were also no reports of fire following the impact.
The Transportation Safety Board of Canada (TSB) was notified of the occurrence and began collecting information to determine the appropriate scope of its investigation. Canadian aviation investigators routinely assess such occurrences before deciding whether to launch a full investigation.
The incident temporarily drew a significant emergency response to the rural area east of High River Regional Airport. No injuries were reported on the ground, and authorities did not indicate any damage to nearby property.
As of the latest available information, investigators have not released any preliminary findings or probable cause, and no further updates on the condition of the injured men have been made public.
Two Injured After Small Aircraft Crashes Near High River Regional Airport In Alberta
A Small Plane Has Crashed N.E. Of Spirit Lake Airport
Explore Okoboji
***NOTE: This story has been updated from a previous version with updated information***
(Okoboji)– A small plane has crashed late this (Saturday, July 4th) morning just northeast of the Spirit Lake airport.
KUOO news has learned it was just the pilot that was
onboard and he managed to walk away from the wreckage uninjurred. He was identified as 72-year-old Kenneth Kemna of North Fort Meyers, Florida.
According to the Dickinson County Sheriff’s Office, authorities were called to the scene just west of Kenue Park and the Dickinson County Nature Center around 10:43 am. They say Kemna had just taken off from the Spirit Lake Airport when the plane sustained a mechanical issue and crashed in a grassy area.
The Arnolds Park-Okoboji Fire and Rescue and Milford Fire Department along with the Dickinson County Sheriff’s Office and the Spirit Lake, Arnolds Park, Milford, and Okoboji Police Departments responded to the scene. The Dickinson County Communications Center and Dickinson County Emergency Management also responded.
Firefighters were cleaning up some fuel that was leaking from the plane.
The Federal Aviation Administration and National Transportation Safety Board are now investigating.
Fireworks Strike Delta Jet
Fourth Of July Landing Takes An Unexpected Turn At Chicago Midway
A routine holiday arrival became anything but ordinary in

Screenshot
the final moments before touchdown. The flight crew reported hearing a loud bang after a firework apparently struck the aircraft during it's descent. The safe landing underscores both the professionalism of the crew and the unexpected hazards that can emerge close to the ground.
A Delta Air Lines Airbus A319 operating Flight DL1076 from Atlanta to Chicago Midway International Airport was reportedly struck by a firework while on final approach shortly before 8:40 p.m. local time on July 4th. According to air traffic control recordings, the aircraft was about 200 feet above the ground when the crew reported, "We just had a firework hit our plane," before continuing the approach and landing safely without declaring an emergency.
After arriving at the gate, the pilots told controllers, "We just heard a bang on the plane, so we'll have to look at it when we get to the gate. We're just hoping it was just a mortar that went off underneath, but definitely felt a big bang." Controllers advised the crew that multiple reports of fireworks near the airport approach path had already been received and that local authorities would be notified.

Delta confirmed the aircraft made contact with a firework during descent and said the A319, registered N316NB, was removed from service for inspection. No injuries were reported among passengers or crew, and the extent of any damage has not been disclosed.
While direct firework strikes on commercial airliners remain exceptionally uncommon, the event highlights a genuine aviation safety concern. Fireworks near airport approach and departure corridors can distract flight crews during the most critical phases of flight, create foreign object debris on airport surfaces, and in rare cases pose a threat to aircraft structures or engines. During one of the busiest Independence Day travel periods on record, the incident served as a powerful reminder that hazards on the ground can reach far higher than many people realize.
NTSB Prelim: Boeing E75
(Witness) Heard A Loud “Pop,” And The Engine Noise Ceased. The Airplane Subsequently Impacted A Hay Field
Location: Dresden, OH Accident Number: ERA26LA224
Date & Time: May 29, 2026, 11:53 Local Registration: N181RF
Aircraft: Boeing E75 Injuries: 2 Serious
Flight Conducted Under: Part 91: General aviation - Personal
On May 29, 2026, about 1153 eastern daylight time, a Boeing E75, N181RF, was substantially damaged when it was involved in an accident near Dresden, Ohio. The pilot and passenger were seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
A witness, who lived near the accident site with her husband, reported that she was standing in her yard and observed the accident airplane fly over her residence in a north direction. She then heard a loud “pop,” and the engine noise ceased. The airplane subsequently impacted a hay field at her neighbor’s residence across the street. Her husband ran to the wreckage to render assistance to the occupants.
Initial examination of the wreckage by an FAA inspector revealed that it came to rest upright in the field, and both the upper and lower right wings sustained substantial damage.
The wreckage was retained for further examination.
FMI: www.ntsb.gov
NTSB Final Report: Luscombe 8E
During The Initial Climb, The Airplane Encountered Windshear
Location: Meeker, Colorado Accident Number: CEN26LA169
Date & Time: April 19, 2026, 10:40 Local Registration: N1398K
Aircraft: Luscombe 8E Aircraft Damage: Substantial
Defining Event: Windshear or thunderstorm Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Personal
Analysis: The pilot reported he was attempting to depart from a remote 2,040 ft long airstrip. During the initial climb, the airplane encountered windshear, and the pilot noticed that the vertical speed indicator depicted a decreasing climb rate. The pilot determined that the airplane was unable to out climb the terrain due to the windshear and opted for a straight-ahead forced landing.
The airplane landed in a three-point configuration in tall, thick sagebrush and eventually nosed over, coming to rest inverted. Both wings and fuselage sustained substantial damage. The pilot reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s inability to maintain climb performance and clearance from terrain due to the airplane’s encounter with windshear during takeoff.
FMI: www.ntsb.gov
NTSB Final Report: Beech 65-A90-1
Airplane Impacted The Ground About 150 Feet Short Of The Runway Threshold
Location: Anchorage, Alaska Accident Number: ANC26LA010
Date & Time: January 16, 2026, 14:58 Local Registration: N918MR
Aircraft: Beech 65-A90-1 Aircraft Damage: Substantial
Defining Event: Abnormal runway contact Injuries: 4 None
Flight Conducted Under: Part 91: General aviation - Executive/Corporate
Analysis: The pilot maneuvered the airplane onto the final approach leg of the traffic pattern; he reduced the power to slow the airplane and encountered a significant downdraft or windshear. The airplane impacted the ground about 150 feet short of the runway threshold. The nose and left main landing gear collapsed, and the left wing contacted a snow berm which resulted in substantial damage to the left wing and lower fuselage. The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- The pilot’s failure to attain proper flare during landing resulting in a hard landing short of the runway threshold. Contributing to the accident were gusting wind conditions.
FMI: www.ntsb.gov

Today in History
13 Years ago today: On 6 July 2013 Asiana Airlines flight 214, Boeing 777-200 was destroyed in a landing accident at San Francisco International Airport, California (SFO). There were 291 passengers and 16 crew members on board. Three passengers died and 48 were seriously injured.
| Date: | Saturday 6 July 2013 |
| Time: | 11:28 |
| Type: | Boeing 777-28EER |
| Owner/operator: | Asiana Airlines |
| Registration: | HL7742 |
| MSN: | 29171/553 |
| Year of manufacture: | 2006 |
| Total airframe hrs: | 37120 hours |
| Cycles: | 5388 flights |
| Engine model: | P&W PW4090 |
| Fatalities: | Fatalities: 3 / Occupants: 307 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed, written off |
| Category: | Accident |
| Location: | San Francisco International Airport, CA (SFO) - United States of America |
| Phase: | Landing |
| Nature: | Passenger - Scheduled |
| Departure airport: | Seoul-Incheon International Airport (ICN/RKSI) |
| Destination airport: | San Francisco International Airport, CA (SFO/KSFO) |
| Investigating agency: | NTSB |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:
Asiana Airlines flight 214, Boeing 777-200 was destroyed in a landing accident at San Francisco International Airport, California (SFO). There were 291 passengers and 16 crew members on board. Three passengers died and 48 were seriously injured.
Flight OZ214 originated in Seoul-Incheon International Airport (ICN), South Korea were it departed at 16:35 local Korean time. Destination of the flight was San Francisco, CA.
The weather at San Francisco was fine with 6-7 knot winds and a visibility of 10+ miles. The pilot undergoing initial operating experience was in the left hand seat as Pilot Flying. An instructor pilot was sitting in the right hand seat. The relief first officer was in the jump seat at the time of the approach.
The pilot flying had logged about 9700 flying hours. Flight 214 was his tenth flight leg on a Boeing 777 while undergoing initial operating experience.
The flight was cleared for an approach to runway 28L, the ILS glidepath of which had been declared unserviceable in the current Notam.
The airplane was configured for landing with 30 degrees of flaps and gear down. Target threshold speed was 137 knots. According to preliminary information from the cockpit voice recorder, the crew did not state and anomalies or concerns during the approach. The throttles were at idle and autothrottle armed.
At 1600 feet the autopilot was disengaged. The aircaft descended through an altitude of 1400 ft at 170 kts and slowed down to 149 kts at 1000 feet. 
At 500 feet altitude, 34 seconds prior to impact, the speed dropped to 134 kts, which was just below the target threshold speed. The airspeed then dropped significantly, reaching 118 knots at 200 feet altitude. The instructor pilot reported that he noticed four red PAPI lights and concluded that the autothrottle had not maintained speed.
Eight seconds prior to impact, the throttles were moved forward. Airspeed according to the FDR, was 112 knots at an altitude of 125 feet. Seven seconds prior to impact, one of the crew members made a call to increase speed.
The stick shaker sounded 4 seconds prior to impact. One second later the speed was 103 knots, the lowest recorded by the FDR. One of the crew members made a call for go a around at 1.5 seconds before impact. The throttles were advanced and the engines appeared to respond normally.
The main landing gear and rear fuselage then struck a sea wall, just short of runway 28L. Airspeed was 106 knots. The empennage separated at the rear bulkhead.
The airplane then ballooned, yawed left and spun 360 degrees before it came to rest to the left of runway 28L, 735 m (2400 ft) from the seawall.
A post impact fire occurred when a fuel tank ruptured inboard of the no. 2 engine, spilling fuel on the hot engine, causing it to ignite.
The ILS glidepath for runway 28L and 28R at SFO had been declared unserviceable from June 1 until August 22.
PROBABLE CAUSE:
The National Transportation Safety Board determines that the probable cause of this accident was the flight crew's mismanagement of the airplane's descent during the visual approach, the pilot flying's unintended deactivation of automatic airspeed control, the flight crew's inadequate monitoring of airspeed, and the flight crew's delayed execution of a go-around after they became aware that the airplane was below acceptable glidepath and airspeed tolerances.
Contributing to the accident were;
(1) the complexities of the autothrottle and autopilot flight director systems that were inadequately described in Boeing's documentation and Asiana's pilot training, which increased the likelihood of mode error;
(2) the flight crew's nonstandard communication and coordination regarding the use of the autothrottle and autopilot flight director systems;
(3) the pilot flying's inadequate training on the planning and executing of visual approaches;
(4) the pilot monitoring/instructor pilot's inadequate supervision of the pilot flying; and
(5) flight crew fatigue which likely degraded their performance.
METAR:
17:56 UTC / 10:56 local time:
KSFO 061756Z 21006KT 10SM FEW016 18/10 A2982 RMK AO2 SLP097 T01780100 10183 20128 51005
Wind 210 degrees at 6 knots; Visibility: 10 or more miles; few clouds at 1600 feet AGL; Temperature: 18°C, Dew point: 10°C; Pressure 1010 mb
18:56 UTC / 11:56 local time:
KSFO 061856Z 21007KT 170V240 10SM FEW016 18/10 A2982 RMK AO2 SLP098 T01830100
Wind 210 degrees at 7 knots, varying in direction between 170 and 240 degrees; Visibility: 10 or more miles; few clouds at 1600 feet AGL; Temperature: 18°C, Dew point: 10°C; Pressure 1010 mb

Aircraft Accident Report
Descent Below Visual Glidepath and Impact With Seawall
Asiana Airlines Flight 214
Boeing 777-200ER, HL7742
San Francisco, California
July 6, 2013
National Transportation Safety Board. 2014. Descent Below Visual Glidepath and Impact With Seawall, Asiana Airlines Flight 214, Boeing 777-200ER, HL7742, San Francisco, California, July 6, 2013.
Aircraft Accident Report NTSB/AAR-14/01. Washington, DC.
Abstract: This report discusses the July 6, 2013, accident involving a Boeing 777-200ER, Korean registration HL7742, operating as Asiana Airlines flight 214, which was on approach to runway 28L when it struck a seawall at San Francisco International Airport (SFO), San Francisco, California. Three of the 291 passengers were fatally injured; 40 passengers, 8 of the 12 flight attendants, and 1 of the 4 flight crewmembers received serious injuries. The other 248 passengers, 4 flight attendants, and 3 flight crewmembers received minor injuries or were not injured. The airplane was destroyed.
Safety issues relate to the need for Asiana pilots to adhere to standard operating procedures regarding callouts; reduced design complexity and enhanced training on the airplane’s autoflight system; opportunity at Asiana for new instructors to supervise trainee pilots in operational service during instructor training; guidance for Asiana pilots on use of flight directors during a visual approach; more
manual flight for Asiana pilots; a context-dependent low energy alert; research that examines the injury potential from significant lateral forces in airplane crashes and the mechanism that produces high thoracic spinal injuries; evaluation of the adequacy of slide/raft inertia load certification testing; aircraft rescue and firefighting (ARFF) training for officers in command of an aircraft accident response; guidance on when to use a skin-piercing nozzle on a burning airplane fuselage; integration of the medical supply buses at SFO into the airport’s preparation drills; guidance or protocols for ensuring the safety of passengers and crew at risk of a vehicle strike during ARFF operations; requirements for ARFF staffing; improvements in SFO emergency communications; and increased Federal Aviation Administration (FAA) oversight of SFO’s emergency procedures manual. Safety recommendations are addressed to the FAA, Asiana Airlines, Boeing, the ARFF Working Group, and the City of San Francisco.
https://www.ntsb.gov/investigations/AccidentReports/Reports/AAR1401.pdf
