We close out this week with the following stories...
Have a safe weekend!
Tom
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Former NASCAR driver Greg Biffle, his family dead in small plane crash in North Carolina: Officials
By Ayesha Ali and Victoria Arancio
STATESVILLE, N.C. -- Former NASCAR driver Greg Biffle and members of his family died when a small plane crashed and caught fire during landing at the Statesville Regional Airport in North Carolina on Thursday, according to the family and officials.
The North Carolina Highway Patrol said it is awaiting confirmation from the medical examiner, but "it is believed that Mr. Gregory Biffle and members of his immediate family were occupants of the airplane."
Iredell County Sheriff Darren Campbell told ABC News five adults and two children died on the Cessna C550.
"This tragedy has left all of our families heartbroken beyond words," the Biffle, Grossu, Dutton and Lunders families said in a statement.
"Greg and Cristine were devoted parents and active philanthropists whose lives were centered around their young son Ryder and Greg's daughter Emma," the statement said. "Emma was a wonderful human being with a kind soul who was loved by many people. Ryder was an active, curious and infinitely joyful child."
"Dennis Dutton and his son Jack were deeply loved as well, and their loss is felt by all who knew them," the statement continued. "Craig Wadsworth was beloved by many in the NASCAR community and will be missed by those who knew him."
NASCAR said in a statement that it is "devastated by the tragic loss of Greg Biffle, his wife Cristina, daughter Emma, son Ryder, Craig Wadsworth and Dennis and Jack Dutton."
"Greg was more than a champion driver, he was a beloved member of the NASCAR community, a fierce competitor, and a friend to so many," NASCAR said. "His passion for racing, his integrity, and his commitment to fans and fellow competitors alike made a lasting impact on the sport."
"Heartbreaking news out of Statesville," North Carolina Gov. Josh Stein wrote on social media. "Beyond his success as a NASCAR driver, Greg Biffle lived a life of courage and compassion and stepped up for western North Carolina after Hurricane Helene. My heart goes out to all those who lost a loved one in this tragic crash."
The cause of the crash is not known, said John Ferguson, manager of the airport in Statesville, about 50 miles north of Charlotte.
The airport is closed for further notice, Ferguson said, noting that it will take time to get the debris off the runway. The Federal Aviation Administration and National Transportation Safety Board are investigating.
https://abc7.com/post/plane-crashes-catches-fire-landing-statesville-regional-airport-north-carolina/18298055/
Air traffic accident alert at Helsinki Airport – this is what it's all about
The rescue service received an alert about a minor air traffic accident at Helsinki Airport.
IS
The rescue service received an alarm on
Lentoasemantie at 11:45.
Finavia's communications report that there was a minor collision between a vehicle and an aircraft at Helsinki Airport.
The impact occurred while the aircraft was moving on the apron.
No injuries occurred.
According to the rescue service, a push tractor had collided with an airplane.
The Central Uusimaa Rescue Department tells IS that the airport's own staff was able to handle the matter and the rescue department was not needed.
According to information from Finavia Communications, it was an SAS aircraft.
On Friday around noon, FlightRadar24 showed a SAS aircraft stalled near the taxiway. The plane was heading towards Copenhagen.
https://www.is.fi/kotimaa/art-2000011704475.html
Man tries to steal plane from Van Nuys airport, crashes into hangar
by: Lily Dallow, Marc Sternfield
A man broke into a flight school hangar at Van
Nuys Airport early Thursday and tried to steal a plane — only to crash it before getting off the ground, the school’s owner told KTLA.
According to the Federal Aviation Administration, a Cessna 172 struck the side of a hangar at Van Nuys Airport around 5 a.m.
Anthony Nercessian, owner of L.A. Flight Academy, told KTLA’s Jillian Smukler that the suspect somehow got onto airport grounds, broke into the hangar, started the aircraft’s engine and began to roll away, apparently attempting to take off.
Nercessian said the man “taxied about 50 to 60 feet” before slamming into the hangar, causing extensive damage to the plane and the structure, and damaging a Porsche in the process.
Footage from KTLA’s Sky5 shows a single-engine aircraft resting nose-first against the side of a hangar, with visible damage to the structure’s exterior. Several people were later seen inspecting the damage and moving the aircraft into a nearby garage.
“He fled, but I heard he got caught,” Nercessian said, adding that he didn’t know the suspect, who was not hurt. He was later identified as Cefarreno Logan, 37. He was arrested and booked on charges of burglary and theft of an aircraft.
The incident is being investigated by Los Angeles Airport Police and the FBI.
https://ktla.com/news/local-news/fbi-investigating-report-of-stolen-plane-after-crash-at-van-nuys-airport/
NTSB Prelim: Cirrus Design Corp SR22T
During The 7 Second Descent, There Was Another TAWS Alert At Which Time The Engine Remained At Full Power
Location: Lincoln, MT Accident Number: WPR26FA032
Date & Time: October 24, 2025, 21:15 Local Registration: N740TS
Aircraft: Cirrus Design Corp SR22T Injuries: 1 Fatal
Flight Conducted Under: Part 91: General aviation - Personal
On October 24, 2025 at 2115 mountain daylight time, a Cirrus SR22T, N740TS, was destroyed when it was involved in an accident near Lincoln, Montana. The pilot sustained fatal injuries. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.
The pilot’s brother, who was also a partial owner of the airplane, stated they spoke with one another on the telephone a few hours before the pilot departed. He stated that on the day of the accident, the pilot decided he wanted to join him for a hunting trip that started the following morning, and was debating between driving or flying. They decided he would fly to Lincoln Airport (S69), despite never having landed there before, because it was closer to the camp where they would be staying. They briefed the flight together and reviewed the weather. The brother monitored the airplane with live flight tracking data online and arrived at the airport about 2120, observing the runway lights were illuminated, but the airplane was not at the airport.
A video camera located in the town of Lincoln captured footage of the airplane’s lights in its last minute of the flight. The airplane’s recoverable data module (RDM) was recovered from the accident site and preliminary information was downloaded. A review of the data revealed that the airplane departed from the pilot’s home base in Spokane, Washington about 2010. The airplane continued on a direct route southeast to Lincoln at an altitude of 9,700 ft mean sea level (msl). About an hour after departure, the airplane was 17 nm from S69 and the autopilot mode was changed to selected altitude mode (ALTS), which was previously entered to be
6,000 ft.
As the airplane descended into the valley at 2112:39, about 1,150 ft above ground level (agl), the pilot lowered the flaps to 50%. The airplane continued to descend and full flaps (100%) were selected 17 seconds later. The airplane aligned with Highway 200, an east-west oriented road that passed directly through the town of Lincoln. While flying over the highway, descending to an altitude of 150 ft agl, the indicated airspeed was between 77 and 87 kts. The airplane then began a gradual climb and the flaps were retracted to 50%, where they remained until impact.
The airplane passed over the town and momentarily crossed to the south side of the highway as it maneuvered toward the airport. (See Figure 2). At 2114:43 the airplane was north of the runway near midfield about 1,030 ft agl. The airplane then made a left turn near the airport’s beacon light and was on a north heading while descending to 575 ft agl. During the descent, at 2114:51 the Terrain Awareness and Warning System (TAWS) activated. The airplane began to climb 5 seconds later and full power was added about 2115:00. A steep left bank was initiated and the stall warning activated at 2115:06 as the airspeed slowed to 50 kts. Immediately thereafter, the autopilot and yaw damper disconnected. A second stall warning activated and the left-bank continued to steepen while the airplane descended rapidly to the accident site. During the 7 second descent, there was another TAWS alert at which time the engine remained at full power.
The accident site was located on flat terrain in a sparsely populated neighborhood north of the airport. The terrain consisted of soft dirt and there were numerous trees immediately surrounding the accident site. The accident site was at an elevation of about 4,600 ft and located 3,355 ft from the runway surface.
The airplane came to rest with the nose oriented on a northerly heading, opposite the direction of the debris field. The wreckage was scattered over a 275-foot area, with the most distant debris, primarily windscreen fragments, located south of the main wreckage. The majority of the main wreckage had sustained significant thermal damage that was consistent with the post-impact fire.
At the beginning of the debris field was a group of mature aspen trees that were severed at various heights. The damage and cuts in the trees were progressively lower in height moving toward the main wreckage. Close examination of the cuts in the trees revealed that paint chips were embedded in the fresh tree cuts. The left-wing spar was separated about six feet inboard from the wingtip; there was composite material similar in appearance to the spar found embedded in a downed tree top. The left main landing gear was separated from its respective gearbox, consistent with impact with a tree.
The airport was equipped with pilot-activated medium intensity runway lights (MIRL) and a 2-light precision approach path indicator (PAPI) on the left side of runway 04. The lights remained illuminated for 15 minutes after activation. A review of FAA aviation weather camera imagery at the airport revealed that the runway lights were illuminated sometime between 2109-2111.
According to the U.S. Naval Observatory, the phase of the moon was waxing crescent with 11.5% of the moon's visible disk illuminated. Sunset was at 1827 and civil twilight was at 1857.
Moon set was at 1935 and at the time of the accident, the moon was about 14.69° below the horizon (including refraction) on an azimuth (heading) of 244°.
The pilot’s spouse stated that he would frequently take last-minute trips and was very comfortable flying the airplane. She stated that he would often fly at night, although those flights would usually terminate at his home airport, which he was familiar with. A review of the airplane’s historic ADS-B data did not reveal any recent flights that occurred after civil twilight.
FMI: www.ntsb.gov

Today in History
28 Years ago today: On 19 December 1997 Silkair flight 185, a Boeing 737-300, crashed north of Palembang, Indonesia, killing all 104 occupants in what appears to have been an intentional crash.
| Date: | Friday 19 December 1997 |
| Time: | 16:13 |
| Type: | Boeing 737-36N |
| Owner/operator: | Silkair |
| Registration: | 9V-TRF |
| MSN: | 28556/2851 |
| Year of manufacture: | 1997 |
| Total airframe hrs: | 2238 hours |
| Cycles: | 1306 flights |
| Engine model: | CFMI CFM56-3B2 |
| Fatalities: | Fatalities: 104 / Occupants: 104 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed, written off |
| Location: | 56 km N of Palembang - Indonesia |
| Phase: | En route |
| Nature: | Passenger - Scheduled |
| Departure airport: | Jakarta-Soekarno-Hatta International Airport (CGK/WIII) |
| Destination airport: | Singapore-Changi International Airport (SIN/WSSS) |
| Investigating agency: | NTSC |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:
Silkair flight 185, a Boeing 737-300, crashed north of Palembang, Indonesia, killing all 104 occupants in what appears to have been an intentional crash.
At 15:37 Silkair flight MI185 took off from Jakarta-Soekarno Hatta Airport runway 25R with the captain as the handling pilot. The flight received clearance to climb to FL350 and to head directly to Palembang. At 15:47 the aircraft passed FL245. Ten seconds later, the crew requested permission to proceed directly to PARDI. The air traffic controller instructed MI185 to standby, to continue flying directly to Palembang and to report when reaching FL350. At 15:53, MI 185 reported reaching FL350. Subsequently, the controller cleared MI185 to proceed directly to PARDI and to report when abeam Palembang. At 16:05, the cockpit voice recorder ceased recording. At 16:10 the controller informed MI185 that it was abeam Palembang. The controller instructed the aircraft to maintain FL350 and to contact Singapore Control when at PARDI. The crew acknowledged this call. At 16:11:27 the FDR ceased recording. MI 185 was still at FL350 until it started a rapid descent around 16:12:18. The aircraft broke up in flight and crashed into the Musi river delta.
Although not concluded by the Indonesian authorities, it has been suggested by a.o. the US NTSB that the captain may have committed suicide by switching off both flight recorders and intentionally putting the Boeing 737 in a dive, possibly when the first officer had left the flight deck. During 1997 the captain experienced multiple work-related difficulties, particularly during the last 6 months. Also at the time of the accident the captain was experiencing significant financial difficulties, which was disputed by the Indonesian investigators. Coincidentally the accident happened on exactly the same date in 1979 the captain was forced to withdraw from a scheduled Air Force A-4 Skyhawk jet training mission because of a mechanical problem with his aircraft. The other three aircraft continued with the training mission and collided with terrain after encountering bad weather in a mountainous area. All of the pilots on board the aircraft were killed.
FINAL REMARKS:
- The NTSC investigation into the MI 185 accident was a very extensive, exhaustive and complex investigation to find out what happened, how it happened, and why it happened. It was an extremely difficult investigation due to the degree of destruction of the aircraft resulting in highly fragmented wreckage, the difficulties presented by the accident site and the lack of information from the flight recorders during the final moments of the accident sequence.
- The NTSC accident investigation team members and participating organizations have done the investigation in a thorough manner and to the best of their conscience, knowledge and professional expertise, taking into consideration all available data and information recovered and gathered during the investigation.
- Given the limited data and information from the wreckage and flight recorders, the NTSC is unable to find the reasons for the departure of the aircraft from its cruising level of FL350 and the reasons for the stoppage of the flight recorders.
- The NTSC has to conclude that the technical investigation has yielded no evidence to explain the cause of the accident.
The US NTSB responded to the Indonesian investigation report in a letter dated December 11, 2000. The NTSB states that "when all of the investigative evidence is considered, it leads to the conclusions that: 1) no airplane-related mechanical malfunctions or failures caused or contributed to the accident, and 2) the accident can be explained by intentional pilot action. Specifically, a) the accident airplane's flight profile is consistent with sustained manual nose-down flight control inputs; b) the evidence suggests that the cockpit voice recorder (CVR) was intentionally disconnected; c) recovery of the airplane was possible but not attempted; and d) it is more likely that the nose-down flight control inputs were made by the captain than by the first officer."
