We close out this week with the following stories...
Have a safe weekend!
Tom
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Plane with 267 passengers on board crashes into radar at Antalya airport destroying wing and leaving hole in aircraft
Harvey Geh , Foreign News Reporter - Will Stewart
A PLANE with 267 passengers on board has crashed
into a radar at an airport in Turkey – destroying its wing and leaving a hole in the jet’s side.
The Boeing 777-3Q8 Turkish Airlines flight struck the metal structure in Antalya – as oxygen masks came down and overhead compartments flew open.
One person was left injured following the collision on Friday which took place as the plane was taxiing.
Shocking footage showed the jet’s wing torn apart following the terrifying impact.
It also showed the huge red and white antenna collapsed on the runway in the aftermath of the strike.
Oxygen masks were seen dangling from the cabin’s
ceiling.
It is believed the plane’s wing clipped a huge metal antenna which then fell onto the body of the Boeing jet.
The crash sparked an urgent evacuation of the 267 passengers who were seen in further footage disembarking the plane.
Many looked at the jet in shock, with some recording the aftermath of the jaw-dropping impact.
A female passenger who filmed the chaos in the cabin said: “After landing, something broke off in the plane.”
Describing another traveller, she added: “The woman is
hysterical. Even the skin of the plane was torn off… this metal thing, we ran over it.”
Other passengers described the sound of the collision as “frightening”.
Paramedics and firefighters were deployed to the scene to help passengers disembarking via the aircraft stairs.
Turkish Airlines launched a technical investigation into the nightmare ordeal.
Holidaymakers reported a two-hour delay collecting their luggage after the crash.
The Sun has reached out to Turkish Airlines for comment.
It comes after a plane crash in Turkey last December killed eight people, including one of Libya’s top military generals.
Footage showed a flash of light across the sky moments
after contact with the jet was lost.
Turkish authorities confirmed Libya’s army chief of staff Mohammed Ali Ahmed Al-Haddad was a passenger on the plane that crashed shortly after takeoff from Ankara, killing everyone on board.
Al-Haddad was returning from an official trip from the Turkish capital alongside the commander of Libya’s ground forces, the director of its military manufacturing authority, an adviser to the chief of staff and a photographer.
Wreckage of the Falcon 50 type business jet was later found by Turkish security personnel in the Haymana district near Ankara, Turkish Interior Minister Ali Yerlikaya said.
https://www.the-sun.com/news/16491580/plane-crashes-antalya-airport-wing-destroyed/
Pilot killed after small plane crashes into Scioto County home
by: Jackson Lilly, Riley McIlmoyle, Jessica Patterson
SCIOTO COUNTY, Ohio (WOWK) – A pilot has died after a
single-engine plane crashed into a home in Scioto County, EMS officials say.
According to Scioto County Emergency Management Director Larry Mullins, the plane took off from the Greater Portsmouth Regional Airport in Minford Thursday around 10:45 a.m. and crashed into a home in the 1400 block of Bennett Schoolhouse Road in Minford, southeast of the airport.
Mullins said Thursday morning only the pilot was on board, and that EMS officials had confirmed they had died in the crash. On Thursday afternoon, Ohio State Highway Patrol officials identified the pilot as Kurt W. Paulus, 76, of Delaware, Ohio.
The Ohio State Highway Patrol says a witness reported to troopers that they saw the 2006 Cirrus SR20 single-engine plane take off from the airport, swerve left and then appear to be losing control before crashing. Troopers say he was heading to Delaware, Ohio.
According to Mullins, those in the home escaped, but the home is a total loss. Troopers said two people were inside at the time and were not injured.
On Thursday afternoon, the Notre Dame Schools out of Portsmouth, Ohio, announced that the home belonged to one of their principals, and that a relief fund has been set up for the family.
“While we are incredibly grateful that they were able to
escape their home safely, the devastation left behind is overwhelming. In a matter of moments, members of our school community lost so much. The home they built together, filled with years of memories and cherished belongings, was forever changed in an instant,” Notre Dame Schools officials said on social media. “As they begin the long road to recovery, we have an opportunity to surround them with the love, compassion, and support that make our Notre Dame family so special.”
The school system also asked for prayers for the loved ones of Mr. Paulus.
OSHP says the Scioto County Sheriff’s Office, Minford Fire Department and EMS, Columbus Division of Police, Scioto County Emergency Agency, FAA, National Transportation Safety Board and the Salvation Army.
https://www.wvnstv.com/top-stories/one-dead-after-small-plane-crashes-into-scioto-county-home/
Driggs-Reed Memorial Airport operating with shortened runway after pipe burst
By Christina MacIntosh / Environmental Reporter
The Driggs-Reed Memorial Airport will be operating with a runway just over half its normal length for at least the next two months due to damage caused by a ruptured irrigation pipe. 
Airport officials discovered the damage Saturday morning when water bubbled up under the asphalt. That pressurized water damaged the structural integrity of part of the runway, said Doug Self, city administrator for Driggs, Idaho.
After a three-day closure, the airport reopened with a 3,850-foot runway, down from its usual 7,200 feet.
“It does limit who can come in currently,” Self said. “Larger jets might not be able to land.”
The burst pipe came under a week before the inaugural Ridgeview Pro Rodeo, an event presented and funded by the Teton Ridge Ranch Foundation, billionaire Thomas Tull’s nonprofit.
The event was expected to bring in some large jets, Self said.
The closure is “likely causing frustration for a lot of people who expected to fly,” he said.
Large aircraft that planned to land in Driggs now must land at the Idaho Falls Regional Airport or the Jackson Hole Airport. Those passengers can then travel to Teton Valley via road, helicopter or small plane, Self said.
The Jackson Hole Airport has not yet seen any “discernible impacts” from the issues in Driggs, spokesperson Jeremy Barnum said.
To the undiscerning eye, the runway looks fine, Self said. But up close, it’s evident that there’s silt and clay on the surface. The ruptured pipe sent pressurized water — coming from a canal uphill — under the runway. A wave pattern in the asphalt is visible, Self said.
The damage will take hundreds of thousands of dollars to fix. The current plan is to cut a rectangle of damaged area out of the runway, repair the underlying structural support and then repave it. The reopening of the full-length runway will likely take eight to 10 weeks.
The city is still evaluating the extent of the damage. Engineers will begin designing the repair this week. City officials still need to figure out funding for the project and are eyeing Federal Aviation Administration grants, Self said.
Fortunately, there are no other pipes underneath the runway, Self said. The water that once traveled through the pipe, which had been replaced less than 20 years ago, will be redirected to existing concrete culverts under the runway.
“They’re in excellent shape,” Self said. “We have no concern of failure.”
https://www.jhnewsandguide.com/news/teton_valley/local/driggs-reed-memorial-airport-operating-with-shortened-runway-after-pipe-burst/article_9175b587-640b-4b65-9773-17adfc79dc80.html
NTSB Releases Preliminary Report On Akron, Ohio PA28 Accident
Flight Instructor And Student Were Fatally Injured In Crash Of PA-28-180
The preliminary National Transportation Safety Board (NTSB) report on the fatal crash of a training flight near Fulton International Airport (AKR) in Akron, Ohio on May 14 said the Piper PA-28-180 aircraft on a training flight had been practicing landings before going into a steep dive and crashing into a home.
The NTSB report said that during short final, and for reasons unknown, the pilot communicated over the common traffic advisory frequency that he was conducting a go-around, and rejoined the traffic pattern. Reported wind about that time was from 330° at 19 knots, gusting to 32 knots.
The NTSB report said shortly before the crash, “the flight track of the airplane showed that it was about 3/4 mile and perpendicular to the runway consistent with a normal traffic pattern. As the airplane approached the end of the downwind leg, the distance from the runway had decreased to about 1/4 mile. The flight track then showed a right turn of about 15°, widening the distance from the runway. The pilot reported the left base for runway 7 over the common traffic advisory frequency and initiated the left turn; immediately thereafter, the airplane entered a steep, uncontrolled descent.
“Eyewitnesses observed the airplane flying straight and level, then observed the left wing drop followed by a spiraling descent. One witness stated that the airplane did two complete revolutions before appearing to recover from the spin, but the airplane continued to “dive” into the neighborhood. Dashcam video from an automobile parked across the street about 300 ft south of the accident site captured the airplane immediately before impact in a steep non-spinning descent. After the airplane disappeared from view behind trees and houses, a large fireball was observed. Home security footage showed the airplane impact on a residential street, where it slid into the attached garage of a 2-story home, impacting an electric vehicle before coming to rest.”
There was a significant post-impact fire, initially caused by the breached fuel tanks, which spread to the vehicle and structure. The electric vehicles’ batteries were subsequently damaged, resulting in a thermal runway of the lithium-ion batteries and an intense fire that took about 20 minutes to extinguish, according to the Akron City Fire Department.
The wreckage was recovered and retained for further examination by the NTSB.
FMI: www.ntsb.gov
NTSB Final Report: Vertical Aviation Technologies Hummingbird
Pilot Had Previously Contacted The Helicopter Kit Manufacturer About Ethanol In Fuel “Eating Up” The Fuel Bladder In The Helicopter
Location: Spring Branch, Texas Accident Number: CEN24FA167
Date & Time: April 29, 2024, 15:12 Local Registration: N829SH
Aircraft: Vertical Aviation Technologies Hummingbird Aircraft Damage: Destroyed
Defining Event: Unknown or undetermined Injuries: 2 Fatal
Flight Conducted Under: Part 91: General aviation - Air drop
Analysis: The pilot departed in the experimental helicopter with a pilot-rated passenger to perform a golf ball drop for a charity event. Flight track data showed that the beginning of the flight was not captured, as the first data point indicated the helicopter was in flight and was approximately 4.3 miles to the northeast of the departure airport and about 1.8 miles to the northwest of the planned golf ball drop location. The data showed the helicopter flying to the southwest of the first data point. The helicopter continued to travel to the southwest, and it then turned to the southeast where the data terminated shortly thereafter at the accident site, which was located about 1.4 miles to the northwest of the departure airport.
Multiple witnesses near the accident site heard the engine produce sputtering and coughing noises just prior to impact. Security camera footage showed the helicopter impact a grass field in a residential area, in front of a house. A postimpact explosion and fire occurred, which consumed the wreckage.
While no mechanical anomalies were found during the airframe and the engine examination, the examination was limited due to the extensive fire damage present. Multiple golf balls were found in the wreckage, which is indicative that the golf ball drop was not completed. The recovered flight track data showed that the helicopter was possibly flying back to the departure airport; however, the intended flight path was not established.
The pilot had previously contacted the helicopter kit manufacturer about ethanol in fuel “eating up” the fuel bladder in the helicopter and causing the fuel lines to “clog.” The kit manufacturer offered to sell the pilot a new fuel bladder to install in the helicopter, but they never heard back from the pilot. According to the FAA, ethanol in automobile fuel is not compatible with the rubber seals and other materials used in aircraft, which could cause fuel system deterioration and malfunction.
The current helicopter maintenance records were not available for review, and the investigation was unable to determine what maintenance had been performed on the airframe and the engine in the several years prior to the accident. Based upon the statements of multiple witnesses, the engine likely sustained a total loss of engine power, which resulted in a forced landing and a subsequent impact with terrain. While it is possible that the cause of the loss of the engine power may have been due to the deterioration of the fuel system from the presence of ethanol in fuel, the extensive fire damage precluded examination.
Due to heart disease, the pilot was at increased risk of a sudden impairing or incapacitating cardiac event, including angina, arrhythmia, or heart attack. There is no autopsy evidence that such an event occurred. However, such an event does not leave reliable autopsy evidence if it occurs immediately before death.
The pilot’s toxicological results indicated use of gabapentin, which the FAA considers a “do not fly” medication. Based on the gabapentin levels measured in the pilot’s heart blood, he was possibly experiencing some effects from his use of the gabapentin; however, specific effects are uncertain and whether he may have been impaired could not be determined based on the level detected alone.
Probable Cause and Findings: The National Transportation Safety Board determines the probable cause(s) of this accident to be -- A total loss of engine power for undetermined reasons, which resulted in a forced landing and a subsequent impact with terrain.
FMI: www.ntsb.gov

Today in History
76 Years ago today: On 12 June 1950 An Air France Douglas DC-4 crashed into the sea while on approach to Bahrain Airport, Bahrain , killing 46 occupants; 6 survived the accident.
| Date: | Monday 12 June 1950 |
| Time: | 21:15 |
| Type: | Douglas DC-4-1009 |
| Owner/operator: | Air France |
| Registration: | F-BBDE |
| MSN: | 42937 |
| Year of manufacture: | 1946 |
| Fatalities: | Fatalities: 46 / Occupants: 52 |
| Other fatalities: | 0 |
| Aircraft damage: | Destroyed, written off |
| Category: | Accident |
| Location: | 5,5 km SE off Bahrain Airport (BAH) - Bahrain |
| Phase: | Approach |
| Nature: | Passenger - Scheduled |
| Departure airport: | Karachi International Airport (KHI/OPKC) |
| Destination airport: | Bahrain International Airport (BAH/OBBI) |
| Investigating agency: | BEA |
| Confidence Rating: | Accident investigation report completed and information captured |
Narrative:
An Air France Douglas DC-4 crashed into the sea while on approach to Bahrain Airport, Bahrain , killing 46 occupants; 6 survived the accident.
The Air France DC-4 was on a scheduled flight from Saigon to Paris. It took off from Karachi (KHI) for Bahrain (BAH) at 16:05. At 20:42 the aircraft called Bahrain approach control giving its altitude as 6500 feet and requesting clearance to descend. Approach control gave clearance to descend to 2000 feet, altimeter setting of 29.51 inches, visibility 1500 yards (1370 metres).
The airplane overflew the airfield at a height of about 1000 feet. At 21:13 the aircraft called Bahrain tower, saying "down wind leg"; the tower acknowledged and said "ground wind 310/20 knots", the aircraft called the tower at 21:15 hours saying "finals" . The tower controller cleared the flight to land on runway 29. On finals the airplane contacted the water and crashed. The wreckage was found in 12 feet of water, 3,3 miles from the runway end 8 hours after the accident.
Two days later an Air France DC-4 on the same flight leg also crashed while on approach to Bahrain at night, killing 40 occupants.
PROBABLE CAUSE: "The pilot-in-command did not keep an accurate check of his altitude and rate of descent during the timed approach procedure, thus allowing his aircraft to fly into the surface of the sea. The possibility that the pilot-in-command was feeling the effects of fatigue cannot be ruled out. It is recommended that consideration be given to equipping Bahrain Airport with radio landing aids and with suitable runway approach lights."
